Vstromvoyager
New member
- Joined
- Nov 29, 2015
- Messages
- 9
- Reaction score
- 0
- Points
- 1
- Vehicle Year
- 1988
- Vehicle
- Ford
- Engine Size
- 2.9L
Long story short, driving my 88 B2 to the mechanic to have a new exhaust installed and the truck stopped running and wouldn’t restart. Towed it to the shop and he said he would check It out after the exhaust. He gave me a call and said the inertia switch was bad. He knew I liked to work on it myself so he bypassed the switch so I could install a replacement. I pulled the switch and out of curiosity I checked it with an ohm meter. It tested good, or I should say it had continuity. I put it back in and it wouldn’t start. Put the jumper back in and it ran fine. My question, finally, is why does it appear to test good? Am I testing it wrong? Anyone with an answer I would greatly appreciate it.